looks good Rob, when do you plan to have it running?
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Thanks Zach. I'm shooting for about 6 weeks from now. I want to have time to break the motor in and work out any problems before the dunes and a spring trip to Milan drag way. Right now I just want it back so I can quit driving a little Mercury Mistake :silly:
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Rob, what fuel rail is that? Im still tryin to figure what rail and how to hook up my fuel lines on the B2 for my 5.0
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looks good rob!
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Originally Posted by deathbypsi
(Post 1612720)
Rob, what fuel rail is that? Im still tryin to figure what rail and how to hook up my fuel lines on the B2 for my 5.0
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Thanks Rob, part numbe would be awesome. So the lines hook at the rear if Im seeing them correct?
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2 Attachment(s)
Yep the lines hook-up at the back drivers side of the motor. The two fittings are made by Russel, one for the pressure side and one for the return side. Both use a -6 AN hose. This setups has worked great for me.
640870 640900 Here you can see how long the lines are to reach the rail Attachment 118265 And here you can see how the stock mustang fuel rail is, hooks up on the front passengers side. The other thing that changes is the fuel pressure regulator moves from the left to the right side. I have plenty of clearance for it on my intake because I have a spacer on it, but i'm not positive if it clears without a spacer. (I am selling mine for a stock HO intake if your interested.) Attachment 118266 |
I was just lookin at spacers. lol
Shoot me a PM with the info. Found the rail as well locally. |
hey man I'm pretty new here this is the first I've stumbled across pics of your truck - followed the thread through from the beginning, the truck looks great and the amount of work you have put in is amazing. If I ever have cash to blow it'll be on a 2nd gen off road machine, your truck really looks great. Everyone complains they haven't updated the ranger in 10 years - I wish they'd update it by going back to that body style.
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nice work rob, cant wait to see it rip'n around at the dunes again
I can't wait to start working into motor mods myself. But right now suspension is a must |
8 Attachment(s)
Well I have been working on the truck every chance I get but haven't taken to many pictures. The block is completely disassembled, has been cleaned, painted, the cylinders are prepped and ready to go. I had to send my crankshaft out to get ground down .010 inches because there was some scoring on the journals. Will be picking it up tomorrow and start assembly. The heads are finally ported, painted, and fully assembled. The valves were all lapped and the valve springs were shimmed. I also static balanced all of the pistons and rods and they are all within .3 grams of each other. Should make things run pretty smoothly. I made a new lower radiator mount and mocked it all up with my old radiator to get everything spaced also. Also switched the electric fan from a puller to a pusher to free up space in the engine compartment. Hopefully it still provides enough cooler. Should have more pictures this weekend.
Attachment 116412 Attachment 116413 Attachment 116414 Attachment 116415 Attachment 116416 Attachment 116417 Attachment 116418 Attachment 116419 |
Those are looking good Rob I cant wait to see it finished and in action.
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Wow I am not very good at up dating project logs... I did finish the rebuild back in March. Ran into several problems such as 7 of 8 injectors being bad and some small electrical issues. Eventually got all the bugs out and had been running strong until about 6 weeks ago. Developed a bad vibration that got worse with RPM, after a couple weeks of trying to track down the problem I had to pull the motor back out and tear it down.
The main bearings were toast, the number 5 bearing was destroyed and the material went through the rest of the motor. The crankshaft was sent out to be reground and additional 30 thousandths on the mains and 10 thousandths on the rod journals. Just recieved all the parts back from the machine shop yesterday, all the work listed below New Cam Bearings Installed Honed the Cylinders Milled the head surface 10 thousandths Decked the heads 25 thousandths (Yay compression) Align Bored and Honed the Mains R&R the rods Coated the Pistons Skirts Balanced the rotating assembly for 7,000+ RPM SFI Approved Balancer ARP Main Studs Added Tomorrow I will begin putting the motor back together and hope to have it running with in a couple of days. Also just finished up rear disc brake conversion last night, just need to finish bleeding the brakes. Should have some pictures of all the work sometime next week. |
Awesome Rob, hope it goes smooth! cant wait till winter is over and then another dunes meet will be upon us. I think after that run I'll tear down my motor and build it up, It could use it.
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wow that sucks but at least you got it all going back together
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What was the cause of the munched bearing ?
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+1, what the hell happened??
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race wars, thats what happened.
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I'm not 100% percent sure what caused it, but it stemmed from the flywheel area. Near as I can tell the input shaft of the trans had very excessive end play and was pushing on the pilot bearing laterally, which eventually chewed up the Number 5 main. When I would remove the trans and clutch/pressure plate the motor would run smooth up to the limiter, but as soon as the pressure plate was re-installed it would shake to all hell. I tried 2 different clutch setups all with the same result.
I just finished up bleeding the brakes on the truck and about to start re-assembling the motor now! |
Well the truck is back on the road. I fired it up around 3pm today, and it started on the 2nd crank so that was great! Had to chase down some issues like the thermostat being stuck closed... but have most of the kinks worked out. Will try and post pictures soon.
Also, I have the rear disc brakes all set up, but I am having a problem with them being very squishy. The pedal goes down over half way before it starts to engage. It stops, but not very well. I have bled the entire system and get nice clean fluid out with no air bubbles on all four corners but it remains soft, so if anyone has any ideas. |
nice work! yeah I kinda have that problem too with my brakes. I bled them great but its still meh out back.
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Did you use new calipers or used lines? It helps to tap on the caliper while bleed as little air bubbles like to stick on the insides of the piston in the caliper...
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What master you using? I would run one off a Ex that had rear disc as it prolly has a smaller bore cylinder.
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8 Attachment(s)
Originally Posted by Dangerranger01
(Post 1726614)
Did you use new calipers or used lines? It helps to tap on the caliper while bleed as little air bubbles like to stick on the insides of the piston in the caliper...
Originally Posted by deathbypsi
(Post 1726732)
What master you using? I would run one off a Ex that had rear disc as it prolly has a smaller bore cylinder.
So far I have 125 miles on them and it stops fine but my foot goes so bloody far down before it engages. But the truck has been driving good today, already have an exhaust leak... so I will chase that down tomorrow, but overall its feeling pretty strong and haven't had any other problems. Now to put a bunch of miles on it before i head to the dunes in 2 weeks. Here are a couple pictures of the shortblock as I put it back together, hopefully will have some complete and shinny pics in a week or so, need to paint my new bed cap and get it mounted. Attachment 100592 Attachment 100593 Attachment 100594 Attachment 100595 Attachment 100596 Attachment 100597 Attachment 100598 Attachment 100599 |
Looks mint,have fun at the dunes! Lucky
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