My GT Finally on the Dyno
My GT Finally on the Dyno
Well guys and gals, it's been a while. I've been covered up with work, which is a good thing, and just been generally busy.
After about 15 pulls, 2 fuel pumps lost, bad plugs, clogged breather valve, new fuel lines, blown fuel rail sensor, falsely marked injectors, and just a few other things...we finally got to this pull lol.
Still have plenty of stuff to do, but it runs pretty nicely for now.
After about 15 pulls, 2 fuel pumps lost, bad plugs, clogged breather valve, new fuel lines, blown fuel rail sensor, falsely marked injectors, and just a few other things...we finally got to this pull lol.
Still have plenty of stuff to do, but it runs pretty nicely for now.
I rewatched it just to make sure, and I didn't notice anything. Something from Kenny Brown or H&R would have to be broken if I did.
No saying that, they are notorious for breaking TQ boxes...but mine are boxed and welded and if they were broke, let's just say it would move more then a bit lol.
Thanks for the compliments guys. Can't wait to get the little things done and clean her up from almost 3 months of shop dust from 3 different locations lol.
I can tell you what it made with no timing, 10.x AFR, and the pump taking a crap on the rollers. Breaking up all the way and shutting down at 3900rpms it made 331/350. Makes just a 'bit' more now lol. Comes in around 10.3psi of boost.
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graniteguy
4.0L OHV & SOHC V6 Tech
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Sep 20, 2005 12:44 AM






